DBC-05 Triple XHP-50.2 Scratch Build !NOW XHP-70.2!

So where can I find those? I wanna melt something! :smiley:

Well just awesome!
so cool these really build from stock bars projects, but so far out of reach for us mere mortals :wink:

Couple of years ago I was bolting bar stock to my drill and using a rotary tool to cut out what I wanted. Now I use the 10x22 lathe in much the same manner. lol
All Professionals are trained amateurs. Everybody starts somewhere, me? I just have to keep starting with my horrid memory…

I make my share of mistakes, like when I was making this simple spacer with one step to go between the retaining ring and pcb of the switch… in that last split second when you expect the part to fall in your hand it does the unexpected and flips over, jamming the lathe to a complete stop and mangling the last 30 minutes of careful work. And so it goes…

Looks sweet pal! More like a piece of art than a torch.

Shame you cant buy many unorthodox designs (i’d love to turn one but i don’t have access to the equipment)

Gorgeous job once again Dale!! You need those SAM 21700's. Can you make be a 3Px2S 21700 battery tube for my 16X?

Wow this has to be my fav of all your scratch builds. The looks is just awesome. You really gone a long ways, I can totally see the improvements in design and total build.
Keep up the great work!

Ahh beautiful, making me really want one of your customs!

Tom, that’s something I have yet to learn. Offset turning. I have the 6” 4 jaw chuck and the offset plate but don’t know how to set it all up. Figured I’d get there one of these days but haven’t so far. Maybe MRsDNF will take another vacay and swing by and show me how all that works. :wink: I could of course run up to North-West Texas and get Dan to walk me through all that.

Its not as hard using a four jaw chuck as it seems Dale. Some marking out and a centre pop where the centre of the hole is. With a centre in the tailstock run it up to the work piece and adjust the jaws until your centre pop mark is central to the centre in the tailstock.

We have all watched what you can do dale and I have 100% faith in your abilities to be able to do this. You are a natural. :+1:

Super nice work Dale!! Thanks for sharing the build. TL

So much amazing goodness going on in this build.

Wow, this is amazing!

Wow, if you hit 12 A it will only be briefly as the cells drop to 3.6V almost immediately. :person_facepalming: silly me, might get more than an hour at 12 A.

The talent on BLF never ceases to amaze me , amazing stuff……………wow

Wow!! Truly impressive!!

Dale how do you keep the switch from liquidizing? Not that your madness needs coaching. You still have that Trustfire TR-J20? Think triple 20700 stacked 4 high, 3x4. Twelve XHP50.2 42000 lumen. Just idle thinking.

nice.

you making some for sale Dale?

Fantastic work Dale. I’m a little jealous as my lathe is in the middle of upgrades. I bought a bicycle sprocket to use as an indexing plate but the centre hole is not quite as centre as I’d like. So I need to fit a 4 jaw chuck to hold it and work it a bit, that in turn requires the backplate to be machined to fit. I keep thinking to myself this would be much easier if everything was already set up on the lathe :person_facepalming: :person_facepalming:

Anyway love your light :+1:

Thats very nice work.
Did you build it as something in between a flooder and a thrower? Like a general purpose light?

I’m thinking all that copper would be good for some xhp70’s, but you probably already have a triple xhp70, right? Lol

Yeah, when Dale said the 20700’s weren’t performing like he thought they should, so he made it a 26650 light, I immediately thought of this review, where HKJ said these 21700’s outperform a 26650 for high amps. Dale, you were so close. You already said your first tube could fit the 21700’s. Now, you’ve got a regression it seems! Well, at least 21700’s will fit in the 26650 tube using a sleeve, as long as you made the tube long enough. You did make it long enough, right?